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72 PINTO WAGON

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New front rotors and everything for '74-'80
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Why the Ford Pinto didn’t suck

Why the Ford Pinto didn't suckThe Ford Pinto was born a low-rent, stumpy thing in Dearborn 40 years ago and grew to become one of the most infamous cars in history. The thing is that it didn't actually suck. Really.

Even after four decades, what's the first thing that comes to mind when most people think of the Ford Pinto? Ka-BLAM! The truth is the Pinto was more than that — and this is the story of how the exploding Pinto became a pre-apocalyptic narrative, how the myth was exposed, and why you should race one.

The Pinto was CEO Lee Iacocca's baby, a homegrown answer to the threat of compact-sized economy cars from Japan and Germany, the sales of which had grown significantly throughout the 1960s. Iacocca demanded the Pinto cost under $2,000, and weigh under 2,000 pounds. It was an all-hands-on-deck project, and Ford got it done in 25 months from concept to production.

Building its own small car meant Ford's buyers wouldn't have to hew to the Japanese government's size-tamping regulations; Ford would have the freedom to choose its own exterior dimensions and engine sizes based on market needs (as did Chevy with the Vega and AMC with the Gremlin). And people cold dug it.

When it was unveiled in late 1970 (ominously on September 11), US buyers noted the Pinto's pleasant shape — bringing to mind a certain tailless amphibian — and interior layout hinting at a hipster's sunken living room. Some call it one of the ugliest cars ever made, but like fans of Mischa Barton, Pinto lovers care not what others think. With its strong Kent OHV four (a distant cousin of the Lotus TwinCam), the Pinto could at least keep up with its peers, despite its drum brakes and as long as one looked past its Russian-roulette build quality.

But what of the elephant in the Pinto's room? Yes, the whole blowing-up-on-rear-end-impact thing. It all started a little more than a year after the Pinto's arrival.

 

Grimshaw v. Ford Motor Company

On May 28, 1972, Mrs. Lilly Gray and 13-year-old passenger Richard Grimshaw, set out from Anaheim, California toward Barstow in Gray's six-month-old Ford Pinto. Gray had been having trouble with the car since new, returning it to the dealer several times for stalling. After stopping in San Bernardino for gasoline, Gray got back on I-15 and accelerated to around 65 mph. Approaching traffic congestion, she moved from the left lane to the middle lane, where the car suddenly stalled and came to a stop. A 1962 Ford Galaxie, the driver unable to stop or swerve in time, rear-ended the Pinto. The Pinto's gas tank was driven forward, and punctured on the bolts of the differential housing.

As the rear wheel well sections separated from the floor pan, a full tank of fuel sprayed straight into the passenger compartment, which was engulfed in flames. Gray later died from congestive heart failure, a direct result of being nearly incinerated, while Grimshaw was burned severely and left permanently disfigured. Grimshaw and the Gray family sued Ford Motor Company (among others), and after a six-month jury trial, verdicts were returned against Ford Motor Company. Ford did not contest amount of compensatory damages awarded to Grimshaw and the Gray family, and a jury awarded the plaintiffs $125 million, which the judge in the case subsequently reduced to the low seven figures. Other crashes and other lawsuits followed.

Why the Ford Pinto didn't suck

Mother Jones and Pinto Madness

In 1977, Mark Dowie, business manager of Mother Jones magazine published an article on the Pinto's "exploding gas tanks." It's the same article in which we first heard the chilling phrase, "How much does Ford think your life is worth?" Dowie had spent days sorting through filing cabinets at the Department of Transportation, examining paperwork Ford had produced as part of a lobbying effort to defeat a federal rear-end collision standard. That's where Dowie uncovered an innocuous-looking memo entitled "Fatalities Associated with Crash-Induced Fuel Leakage and Fires."

The Car Talk blog describes why the memo proved so damning.

In it, Ford's director of auto safety estimated that equipping the Pinto with [an] $11 part would prevent 180 burn deaths, 180 serious burn injuries and 2,100 burned cars, for a total cost of $137 million. Paying out $200,000 per death, $67,000 per injury and $700 per vehicle would cost only $49.15 million.

The government would, in 1978, demand Ford recall the million or so Pintos on the road to deal with the potential for gas-tank punctures. That "smoking gun" memo would become a symbol for corporate callousness and indifference to human life, haunting Ford (and other automakers) for decades. But despite the memo's cold calculations, was Ford characterized fairly as the Kevorkian of automakers?

Perhaps not. In 1991, A Rutgers Law Journal report [PDF] showed the total number of Pinto fires, out of 2 million cars and 10 years of production, stalled at 27. It was no more than any other vehicle, averaged out, and certainly not the thousand or more suggested by Mother Jones.

Why the Ford Pinto didn't suck

The big rebuttal, and vindication?

But what of the so-called "smoking gun" memo Dowie had unearthed? Surely Ford, and Lee Iacocca himself, were part of a ruthless establishment who didn't care if its customers lived or died, right? Well, not really. Remember that the memo was a lobbying document whose audience was intended to be the NHTSA. The memo didn't refer to Pintos, or even Ford products, specifically, but American cars in general. It also considered rollovers not rear-end collisions. And that chilling assignment of value to a human life? Indeed, it was federal regulators who often considered that startling concept in their own deliberations. The value figure used in Ford's memo was the same one regulators had themselves set forth.

In fact, measured by occupant fatalities per million cars in use during 1975 and 1976, the Pinto's safety record compared favorably to other subcompacts like the AMC Gremlin, Chevy Vega, Toyota Corolla and VW Beetle.

And what of Mother Jones' Dowie? As the Car Talk blog points out, Dowie now calls the Pinto, "a fabulous vehicle that got great gas mileage," if not for that one flaw: The legendary "$11 part."

Why the Ford Pinto didn't suck

Pinto Racing Doesn't Suck

Back in 1974, Car and Driver magazine created a Pinto for racing, an exercise to prove brains and common sense were more important than an unlimited budget and superstar power. As Patrick Bedard wrote in the March, 1975 issue of Car and Driver, "It's a great car to drive, this Pinto," referring to the racer the magazine prepared for the Goodrich Radial Challenge, an IMSA-sanctioned road racing series for small sedans.

Why'd they pick a Pinto over, say, a BMW 2002 or AMC Gremlin? Current owner of the prepped Pinto, Fox Motorsports says it was a matter of comparing the car's frontal area, weight, piston displacement, handling, wheel width, and horsepower to other cars of the day that would meet the entry criteria. (Racers like Jerry Walsh had by then already been fielding Pintos in IMSA's "Baby Grand" class.)

Bedard, along with Ron Nash and company procured a 30,000-mile 1972 Pinto two-door to transform. In addition to safety, chassis and differential mods, the team traded a 200-pound IMSA weight penalty for the power gain of Ford's 2.3-liter engine, which Bedard said "tipped the scales" in the Pinto's favor. But according to Bedard, it sounds like the real advantage was in the turns, thanks to some add-ons from Mssrs. Koni and Bilstein.

"The Pinto's advantage was cornering ability," Bedard wrote. "I don't think there was another car in the B. F. Goodrich series that was quicker through the turns on a dry track. The steering is light and quick, and the suspension is direct and predictable in a way that street cars never can be. It never darts over bumps, the axle is perfectly controlled and the suspension doesn't bottom."

Need more proof of the Pinto's lack of suck? Check out the SCCA Washington, DC region's spec-Pinto series.

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My Somewhat Begrudging Apology To Ford Pinto

ford-pinto.jpg

I never thought I’d offer an apology to the Ford Pinto, but I guess I owe it one.

I had a Pinto in the 1970s. Actually, my wife bought it a few months before we got married. The car became sort of a wedding dowry. So did the remaining 80% of the outstanding auto loan.

During a relatively brief ownership, the Pinto’s repair costs exceeded the original price of the car. It wasn’t a question of if it would fail, but when. And where. Sometimes, it simply wouldn’t start in the driveway. Other times, it would conk out at a busy intersection.

It ranks as the worst car I ever had. That was back when some auto makers made quality something like Job 100, certainly not Job 1.

Despite my bad Pinto experience, I suppose an apology is in order because of a recent blog I wrote. It centered on Toyota’s sudden-acceleration problems. But in discussing those, I invoked the memory of exploding Pintos, perpetuating an inaccuracy.

The widespread allegation was that, due to a design flaw, Pinto fuel tanks could readily blow up in rear-end collisions, setting the car and its occupants afire.

People started calling the Pinto “the barbecue that seats four.” And the lawsuits spread like wild fire.

Responding to my blog, a Ford (“I would very much prefer to keep my name out of print”) manager contacted me to set the record straight.

He says exploding Pintos were a myth that an investigation debunked nearly 20 years ago. He cites Gary Schwartz’ 1991 Rutgers Law Review paper that cut through the wild claims and examined what really happened.

Schwartz methodically determined the actual number of Pinto rear-end explosion deaths was not in the thousands, as commonly thought, but 27.

In 1975-76, the Pinto averaged 310 fatalities a year. But the similar-size Toyota Corolla averaged 313, the VW Beetle 374 and the Datsun 1200/210 came in at 405.

Yes, there were cases such as a Pinto exploding while parked on the shoulder of the road and hit from behind by a speeding pickup truck. But fiery rear-end collisions comprised only 0.6% of all fatalities back then, and the Pinto had a lower death rate in that category than the average compact or subcompact, Schwartz said after crunching the numbers. Nor was there anything about the Pinto’s rear-end design that made it particularly unsafe.

Not content to portray the Pinto as an incendiary device, ABC’s 20/20 decided to really heat things up in a 1978 broadcast containing “startling new developments.” ABC breathlessly reported that, not just Pintos, but fullsize Fords could blow up if hit from behind.

20/20 thereupon aired a video, shot by UCLA researchers, showing a Ford sedan getting rear-ended and bursting into flames. A couple of problems with that video:

One, it was shot 10 years earlier.

Two, the UCLA researchers had openly said in a published report that they intentionally rigged the vehicle with an explosive.

That’s because the test was to determine how a crash fire affected the car’s interior, not to show how easily Fords became fire balls. They said they had to use an accelerant because crash blazes on their own are so rare. They had tried to induce a vehicle fire in a crash without using an igniter, but failed.

ABC failed to mention any of that when correspondent Sylvia Chase reported on “Ford’s secret rear-end crash tests.”

We could forgive ABC for that botched reporting job. After all, it was 32 years ago. But a few weeks ago, ABC, in another one of its rigged auto exposes, showed video of a Toyota apparently accelerating on its own.

Turns out, the “runaway” vehicle had help from an associate professor. He built a gizmo with an on-off switch to provide acceleration on demand. Well, at least ABC didn’t show the Toyota slamming into a wall and bursting into flames.

In my blog, I also mentioned that Ford’s woes got worse in the 1970s with the supposed uncovering of an internal memo by a Ford attorney who allegedly calculated it would cost less to pay off wrongful-death suits than to redesign the Pinto.

It became known as the “Ford Pinto memo,” a smoking gun. But Schwartz looked into that, too. He reported the memo did not pertain to Pintos or any Ford products. Instead, it had to do with American vehicles in general.

It dealt with rollovers, not rear-end crashes. It did not address tort liability at all, let alone advocate it as a cheaper alternative to a redesign. It put a value to human life because federal regulators themselves did so.

The memo was meant for regulators’ eyes only. But it was off to the races after Mother Jones magazine got a hold of a copy and reported what wasn’t the case.

The exploding-Pinto myth lives on, largely because more Americans watch 20/20 than read the Rutgers Law Review. One wonders what people will recollect in 2040 about Toyota’s sudden accelerations, which more and more look like driver error and, in some cases, driver shams.

So I guess I owe the Pinto an apology. But it’s half-hearted, because my Pinto gave me much grief, even though, as the Ford manager notes, “it was a cheap car, built long ago and lots of things have changed, almost all for the better.”

Here goes: If I said anything that offended you, Pinto, I’m sorry. And thanks for not blowing up on me.

My Cruiser Wagon Project.....

Started by TIGGER, July 31, 2006, 12:23:06 AM

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TIGGER

Here are a couple pictures of the 79 Bobcat that I picked up a couple weeks ago.  I wanted to buy this car a couple years ago but the gentleman that owned it did not want to part with it.  It is a 2.3L 4spd car, deluxe interior, ralley wheels, factory tach and gauges.  He had wrecked it pretty good and had it towed to his sisters house.  It was there that I found it.  I ended up selling him the fender and some misc parts to get it legal but he never did anything with it.  He passed away earlier this year and I bought it from his estate.  The straightest panel is the fender I hung on it.  All the rest have dents.  The radiator core support is all bent as well.  I had to beat it out with a sledge hammer to get the radiator back in it without the fan hitting it.  I will eventually part it out but for now it will help me fix the wiring as all the idiot lights and gauges are working.
79 4cyl Wagon
73 Turbo HB
78 Cruising Wagon (sold 8/6/11)

TIGGER

Here are a couple more pictures of the engine compartment.
79 4cyl Wagon
73 Turbo HB
78 Cruising Wagon (sold 8/6/11)

TIGGER

I had some time today so I pulled the motor and transmission.  I also cleaned up the engine compartment as best I could before the rain started.  I am not sure what I am going to do with the engine compartment.  I have not found a shade of orange in rattle can that I like.  I also seam sealed the seam where the cowl and firewall meet.  Hopefully this solves my water leak problem.  I have some wiring to fix.  The idiot lights and temp gauge did not work.  After pulling the motor I found out why.  I hope to have some more time to work on it over this weekend.  Here are some pictures.
79 4cyl Wagon
73 Turbo HB
78 Cruising Wagon (sold 8/6/11)

TIGGER

Thanks High_Horse I hope it turns out like I want it.
79 4cyl Wagon
73 Turbo HB
78 Cruising Wagon (sold 8/6/11)

High_Horse

Tigger,
      Your doing good and you a working with a very nice speciman of a Crusing wagon.
Disclaimer......I am not just saying that cause I am a wagon owner.
ThunderPinto and I are looking forward with riding with you one day as we are with all the Pintos on this sight.

                                                                                         High_Horse
                                                                                           #226
Started with a Bobcat wagon. Then a Cruising wagon. Now a Chocolate brown 77 wagon. I will enjoy this car for a long time. I'm in. High_Horse

TIGGER

Here is the doner panel.  It will have to be trimmed as it is a little bigger than the piece I cut out.
79 4cyl Wagon
73 Turbo HB
78 Cruising Wagon (sold 8/6/11)

TIGGER

Here is a picture of the hole and the panel I cut out.
79 4cyl Wagon
73 Turbo HB
78 Cruising Wagon (sold 8/6/11)

TIGGER

Another picture of the engine and what is left of the engine that is still in the car.  I have not decided if I will paint the engine compartment or not.  I can't seem to find a bright orange in rattle can :(  It may end up being black ::)  I have not decided yet.
79 4cyl Wagon
73 Turbo HB
78 Cruising Wagon (sold 8/6/11)

TIGGER

I pretty much finished the engine last night.  There is not much else to put on.  I am using all the factory clips and fasteners that I can find.  I will use my 79 wagon to route the vacuum lines when the time comes.  Tonight I was going to start pulling the transmission but I am short two jackstands.  My 67 Mustang is currently using my other pair.  I will need to pick up another pair.  I ended up pulling some things like the exhaust and shifter but it was a little tight for me.  I also fixed the parking brake.  The car was missing the adjusting rod and cable bracket when I bought it.  I have had the parts for a year now but never got around to installing it.  Once I was done with that, I started fooling with the floorboard rust.  I ended up cutting out the rear section.  It went fairly quick.  The longest part was the spot welds around the leaf spring bracket.  Here are a couple pictures of the engine.
79 4cyl Wagon
73 Turbo HB
78 Cruising Wagon (sold 8/6/11)

TIGGER

More pics
79 4cyl Wagon
73 Turbo HB
78 Cruising Wagon (sold 8/6/11)

TIGGER

I put the wagon in the garage over the weekend.  I started pulling off stuff off tonight.  The alternator and power steering pump was being held on by three bolts.  All were very loose and came out by hand, not good.  In addition to the loose bolts, I found some broken wires.  This is the reason why the temperature gauge does not work and who know what else.  I also think I found part of the source of my water leak.  The seam sealer is missing on the pinch seam along the firewall.  I had a similar problem on my 67 Mustang between the cowl and kickpanel.  I will pick up some seam sealer tomorrow and take care of it.
79 4cyl Wagon
73 Turbo HB
78 Cruising Wagon (sold 8/6/11)

TIGGER

BTW, this is Tigger
79 4cyl Wagon
73 Turbo HB
78 Cruising Wagon (sold 8/6/11)

TIGGER

Last night I pulled the oil pan and replaced the rear main seal as well as the oil pan gasket.  Today I installed a new timing belt and put all the sheetmetal back on the engine.  I then did a final cleaning and painted it.  Here are a couple pics of the finished product.  The engine out of the wagon will donate the rest of the parts as the exhaust manifold off this motor had a crack.  Sometime in the next couple weeks I will kick Tigger outside and pull the wagon into the garage for the motor and transmission swap.
79 4cyl Wagon
73 Turbo HB
78 Cruising Wagon (sold 8/6/11)

TIGGER

Here are a couple pictures after stripping it and washing it down with 4 cans of Gunk.
79 4cyl Wagon
73 Turbo HB
78 Cruising Wagon (sold 8/6/11)

TIGGER

I pulled the motor from my parts car a couple weekends ago.  Here are a couple pictures of what it looked like when it came out. 

I found a bunch of receipts behind the glove box of my parts car when I removed the dash.  It is looking like this engine had 86K on it when the timing belt jumped a tooth.  My parts car spent the first 14 years of its life as a campus security car for a local Hi-tech company here in Beaverton.  From the receipts it looks like the car had about 26K in the mid 90's.
79 4cyl Wagon
73 Turbo HB
78 Cruising Wagon (sold 8/6/11)

TIGGER

I installed my slots today and washed it real quick.  It looks shiny ;D because it is still wet.
79 4cyl Wagon
73 Turbo HB
78 Cruising Wagon (sold 8/6/11)

TIGGER

Thanks, Orange is my favorite color.  The car is very similar to the one on the cover, it is just missing the aluminum slots, which I have.  I have one left to polish and then I will install them.  They already have tires so it should be quick and easy.  Maybe I will throw them on tonight.
79 4cyl Wagon
73 Turbo HB
78 Cruising Wagon (sold 8/6/11)

dholvrsn

I like the color!

BTW, did I ever thell you that my Grandpa was the Allis Chalmers dealer in Moorhead, Iowa? ;D

Yours also looks like a ringer for the CW on the cover of the '77 edition of Petersen's Complete Book of Pinto.
'80 MPG Pony, '80-'92
'79 porthole wagon, '06-on
'80 trunk model. '17-on
-----
'98 Dodge Ram 1500
'95 Buick Riviera
'63 Studebaker Champ
'57 Studebaker Silver Hawk
'51 Studebaker Commander Starlight
'47 Studebaker Champion
'41 Studebaker Commander Land Cruiser

TIGGER

Here is a picture of the seat without the cheesy seat cover.  I also include a picture of my parts car that will donate its floor board and the engine;D  I hope to get some more time with the car tomorrow.
79 4cyl Wagon
73 Turbo HB
78 Cruising Wagon (sold 8/6/11)

TIGGER

Here is the drivers side.  A little time with a wire wheel and some primer should clean things up nicely.
79 4cyl Wagon
73 Turbo HB
78 Cruising Wagon (sold 8/6/11)

TIGGER

Now the ugly.....  It looks like it will need a full pass side floor pan.  The drivers side is solid.  It just has a puncture wound from something.  I can see the scrape marks from below.  Here is the rear and front of the pass side floor board.
79 4cyl Wagon
73 Turbo HB
78 Cruising Wagon (sold 8/6/11)

TIGGER

While doing the brakes I noticed that the passenger side floor board had some holes in it.  I have not found the source of the leak but I decided to pull the carpet and see how bad the floor really is. The replacement carpet was glued on top of the original carpet.  Aparently the drivers side window was broken at one time.
79 4cyl Wagon
73 Turbo HB
78 Cruising Wagon (sold 8/6/11)

TIGGER

I rebuilt the entire brake system shortly after I brought it home.  Other than collecting parts for it I have not done much to it lately.  Today I decided to install some of the part I have aquired over the last year.  I installed the door panels and arm rests.  They are not perfect but are in much better condition than the original ones were.
79 4cyl Wagon
73 Turbo HB
78 Cruising Wagon (sold 8/6/11)

TIGGER

A couple more of when I bought it.
79 4cyl Wagon
73 Turbo HB
78 Cruising Wagon (sold 8/6/11)

TIGGER

Here are some pics of my wagon project.  I bought it about a year and a half ago from a towing auction.  It ran and drove but the brakes were almost non existant which made for an interesting drive home.  The body is decent.  About the only rust I noticed off the bat was in the hatch.  The car had the rear slats at one time but they were removed and the holes were never filled.  Here are some pictures when I brought it home.
79 4cyl Wagon
73 Turbo HB
78 Cruising Wagon (sold 8/6/11)